Well I did it. I threw the chainsaw in the boot, drove 7hs south to the Sportstar and cut the taproot. She is no longer solidly grounded. 😅
I'd waited months for my compliance engineer or anybody sufficiently experienced to do the test flight. It never happened so I left here on Friday morning and arrived in time to do a little maintenance so that it was ready for Saturday morning. The forecast was for SE winds of around 20kts gusting to 40kts but that's fine on a runway 14-32, directly up the runway.
I'd flushed the old fuel and replaced it a few weeks back so this time it fired up straight away. Anybody watching would have thought I took way too long to get underway but I wanted to be sure I'd ticked all the boxes. 13 years out of the air is a long time. The last flight recorded in the logbook was 11/6/2007 but I've found a few loose sheets that added the last 200 hours.
I really wanted a more experienced pilot to take the first flight but I got tired of waiting. Not just because it may have faults but it has a throttle control that I find very difficult to use. Anyway I made the necessary radio calls, followed the run-up procedure and lined up for take-off. To say I was a little nervous was an understatement but all I had to do was push that awful throttle control.
I set the propeller to fine pitch and gently pushed the throttle button all the way home. It leapt off the mark like nothing I've been in before. I reckon I was in the air in less than 100m, undoubtedly the headwind had something to do with that. I had intended to keep it close to the runway for the first stretch incase something went wrong but by the end of the runway the altimeter was showing 600'. At that point I took a glance at the tacho, a little 2" one on the wrong side of the panel, I was a little shocked to see the little Rotax was singing along at 6700rpm, about 900 beyond the red line.
I gave the throttle knob a quick flick anti-clockwise, it did nothing so I quickly pulled some extra pitch on the prop to bring the revs back to about 5000 while continuing to climb. By the time I was over the quarry where we usually reached 500' and turned crosswind I'd hit 1000' so then I had a crack at releasing the throttle. It's awkward pushing the button to release it while pulling it to reduce revs. I can't do it smoothly but it's not so bad when you have time to fiddle with it.
From there it got easier. I headed down-wind in the circuit just to stay close to the airstrip but at this stage I was not confident enough to land so I headed for the training area. At 4000' I thought it safe enough to try some stalls. I guess with my light weight and the lightweight plane I should have expected it but it continued to climb at idle until hitting the bottom line on the airspeed indicator, 30kts before a gentle but distinct fall, no stall warning and no vibration. I tried a couple more but next time I'll see what it does with a couple of notches of flap.
The L2 who helped me put the wings back on and made out the condition report straightened a couple of things that appeared bent in the travel from Queensland. One was the stall warning switch and the other was a fixed trim tab on the RH aileron.
Perhaps neither was actually damaged because now the stall warning doesn't work and it was flying with a heavy right wing. Once on the ground I bent that little trim tab up a little and now it flies level.
Anyhow, eventually I headed back to the airport, can't stay up there forever it seems. Even though I was taught to not use the carby heat I pulled it on when turning base and off half way down final. The wind was gusty but still directly down the airstrip. The airspeed indicator was showing 55kts when I touched down but in reality I was probably only doing 25kts ground speed. There was the tiniest chirp from two tyres but no other feeling. My first thought was I'd bounced but no, I was firmly on the ground after the best landing I've ever done.
I went out again at 6:30pm after the wind dropped and did a few circuits and some great landings. I don't know if it was just the headwind or the Sportstar eager to get back on the ground but all my landings were soft and so much easier than all those previous. This morning I went up again. I flew down to White Gum Park with the intention of filling up at their 98 bowser. When I flew over the airstrip the windsock was stretched directly sideways, perhaps a good 30-40kt cross wind. I decided I was not ready for that so headed back to Northam, parked the plane and drove back home very happy.